- Location
- COMMERCE TWP, MI
OK. I'm frustrated and in need of help. I feel I may have more on my hands than capable of but will try anyway. Last year I bought a motor that was built by #Zero. Great looking motor. It was built with NW sleeve and the specs are as follow the way I am running it now.
Here is where I am at now.
771 bb ported nicely and built by #zero
ada head with 35cc domes. Compression last year when I bought the motor 185-190 psi. Compression after rebuilt and base gasket was 205-210psi. (just checked squish @ .035?)
Just replaced the crank and replaced the cylinder base gasket with an aluminum base gasket.
I rebuilt a set of sbn 44's with an original mikuni rebuilt kits and set the carb up to
120p/125m 2.0 n/s 95g spring(Low 3/4 turn out-high 1-1/8 out)
aftermarket flame arrestors
running a factory b pipe (ported and cleaned) with a blaster mod chamber to an atp waterbox
skat setback mag with a 13/18 cutback impeller from Maniac with a medium cone
I went to water test the ski this past weekend (it was 38 degree w/t) and coasted around a bit to let the ski warm up properly. After about 5-10 minutes of low rpm coasting at about 1/4 throttle I started to play 1/8 throttle - 3/8 throttle making sure to stay under a half throttle pull. The ski brapped pretty nicely but every 3rd or fourth time of pulling the throttle she felt like she would fuel load and gargle pretty bad falling to almost a stall and then take off again. This seem to be a rich condition so we turned to low adjusters into 3/4 and test ran again. Same condition same throttle response. After reading the Mikuni Manuel for the um-teenth time we determined I was looking at possible to low on the pop off pressure and possible to large of a low speed jet. I changed the low speed jet to a 115 in both carbs and changed the pop off pressure to 28 psi with a spring change to 115g.
After putting everything back together and trying to start on the stand my ski wouldn't start and stay running without the primer being used. I pulled the carbs again and reinspected everything, sprayed my filters out and reassembled again. No she is starting but has an unmaintainable idle. Seems very high on one start and low on another start. (throttle cable is not pinched or pulling)
I was advised to check my squish just to know as much about my setup as possible and after checking that tonight it's at .035 which I know is not the ideal spot to be?!
It seems to me I have a bunch of spot that I need to address but could really use some help getting in the right direction so i'm not wasting my time as I'm trying to take this ski to wave daze and time is ticking!!!!
thanks for the HELP to anyone that can and if I missed some detail that needs to be address let me know!
Currently the cylinder head is pulled and the domes are out as I need direction on fixing the squish issue?
Here is where I am at now.
771 bb ported nicely and built by #zero
ada head with 35cc domes. Compression last year when I bought the motor 185-190 psi. Compression after rebuilt and base gasket was 205-210psi. (just checked squish @ .035?)
Just replaced the crank and replaced the cylinder base gasket with an aluminum base gasket.
I rebuilt a set of sbn 44's with an original mikuni rebuilt kits and set the carb up to
120p/125m 2.0 n/s 95g spring(Low 3/4 turn out-high 1-1/8 out)
aftermarket flame arrestors
running a factory b pipe (ported and cleaned) with a blaster mod chamber to an atp waterbox
skat setback mag with a 13/18 cutback impeller from Maniac with a medium cone
I went to water test the ski this past weekend (it was 38 degree w/t) and coasted around a bit to let the ski warm up properly. After about 5-10 minutes of low rpm coasting at about 1/4 throttle I started to play 1/8 throttle - 3/8 throttle making sure to stay under a half throttle pull. The ski brapped pretty nicely but every 3rd or fourth time of pulling the throttle she felt like she would fuel load and gargle pretty bad falling to almost a stall and then take off again. This seem to be a rich condition so we turned to low adjusters into 3/4 and test ran again. Same condition same throttle response. After reading the Mikuni Manuel for the um-teenth time we determined I was looking at possible to low on the pop off pressure and possible to large of a low speed jet. I changed the low speed jet to a 115 in both carbs and changed the pop off pressure to 28 psi with a spring change to 115g.
After putting everything back together and trying to start on the stand my ski wouldn't start and stay running without the primer being used. I pulled the carbs again and reinspected everything, sprayed my filters out and reassembled again. No she is starting but has an unmaintainable idle. Seems very high on one start and low on another start. (throttle cable is not pinched or pulling)
I was advised to check my squish just to know as much about my setup as possible and after checking that tonight it's at .035 which I know is not the ideal spot to be?!
It seems to me I have a bunch of spot that I need to address but could really use some help getting in the right direction so i'm not wasting my time as I'm trying to take this ski to wave daze and time is ticking!!!!
thanks for the HELP to anyone that can and if I missed some detail that needs to be address let me know!
Currently the cylinder head is pulled and the domes are out as I need direction on fixing the squish issue?
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