I haven't changed anything since last September.
Last year I went from bone stock to B-pipe and impeller. Ran great. We start riding in Houston around Feburary. Nice and cool. By August it was hesitating on the low side. Leaned it up and it ran decent, not as snappy as before. I added the head in September and it seemed to help.
This year it started to have a hard time starting. So I went into the electronics box and discoverd it had been leaking for a long time. I clean everything (connections all pulled apart, hit with compressed air and wd40. All cpmponents cleaned and reinstalled) EXTREMELY well Sunday and put it back together. Took it out last night and it has a terrible cough sputter cough cough right off idle. Parr helps me adjust the lows and I think we have them at 3/4 out. Helps but still very noticable.
So I was thinking about going back to the recommended setting and see where that gets me.
Any Ideas?