- Location
- Strathroy Ontario Canada
Hey guys
I am looking for a little input.
I just built a stock stroke big bore, 61x cyl. with 85.5mm pro x pistons. I have dual 44 sbn's on an r&d intake. I'm running a 100 main, 110 low, 2.3n&s with 115g spring. This worked great on my ported 701.
If I do a sub, nose stab or idle, this thing takes a long time to clear out. I rode 1/4 throttle for a min. then hit it. It feels good without being loaded up. My problem is up to 1/4 throttle. The plugs are dark, but dry. I also have alot of piston wash. Would a higher popoff fix any of this?
Thanks
I am looking for a little input.
I just built a stock stroke big bore, 61x cyl. with 85.5mm pro x pistons. I have dual 44 sbn's on an r&d intake. I'm running a 100 main, 110 low, 2.3n&s with 115g spring. This worked great on my ported 701.
If I do a sub, nose stab or idle, this thing takes a long time to clear out. I rode 1/4 throttle for a min. then hit it. It feels good without being loaded up. My problem is up to 1/4 throttle. The plugs are dark, but dry. I also have alot of piston wash. Would a higher popoff fix any of this?
Thanks