701 runs like a stabbed rat for 15-20 seconds, then sounds like it's being choked out.

Just did a top end on my 701. Not my first rodeo with 2 strokes or PWC engines, but my first 701. ADA head, B pipe, single 44 stock 61x bottom end.

It ran great for 15-20 minutes during break in. Then I came back, took a rest, went back out and it ran as per the title. I pulled the head and this is what I saw.

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I changed the needle and seat as per recs, but when I had issues I went back to my original spec and it ran the same. I ran with the hood off to confirm I wasn't choking out the motor with exhaust fumes. Same issue. Checked compression to be sure, 185 both holes. Spark plugs do not look obviously rich.

I am going to test how well my head is sealed tonight to see whether I may be leaking water in. I was just curious what people may think this could be. Do people think that is water or unburnt fuel?

Thnak you
 

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I've learned the hard way to always do a leak down before disassembly and after a rebuild. Never know and it eliminates the possibility. It could have had a very small one that got a little bigger and didn't show it's face until a little later. I don't really think it's your issue but it's always worth checking. You could have something in your ignition system failing after it gets warm.
 

WFO Speedracer

A lifetime ban is like a lifetime warranty !
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Don't feel bad that Seadoo GTS I just finished , I water tested it a few weeks back and it ran perfect but the jet pump had serious cavitation ,I put another pump and wear ring on it , I decided to take it to the river for Labor day since it was full of gas and had just been registered , I started it before I left the house , sounded fine, I put it in the water , it went about 100 yards and died , got it started and back to the bank and completely ran the battery down messing with it , it would crank and run but not idle or come out of the hole .

I said F it and pot it back on the trailer, I pulled the carb apart this morning and found nothing, internal filter was clean everything looked good , I pulled the pilot jet out, perfectly clean , I ran a small wire bent 90 degrees through each bypass hole, then blew cleaner through the pilot circuit and reassembled it , runs like a top , the only thing I can figure is one or more of the bypass holes got stopped up and that's all it takes for it to run like poop.
 
Don't feel bad that Seadoo GTS I just finished , I water tested it a few weeks back and it ran perfect but the jet pump had serious cavitation ,I put another pump and wear ring on it , I decided to take it to the river for Labor day since it was full of gas and had just been registered , I started it before I left the house , sounded fine, I put it in the water , it went about 100 yards and died , got it started and back to the bank and completely ran the battery down messing with it , it would crank and run but not idle or come out of the hole .

I said F it and pot it back on the trailer, I pulled the carb apart this morning and found nothing, internal filter was clean everything looked good , I pulled the pilot jet out, perfectly clean , I ran a small wire bent 90 degrees through each bypass hole, then blew cleaner through the pilot circuit and reassembled it , runs like a top , the only thing I can figure is one or more of the bypass holes got stopped up and that's all it takes for it to run like poop.

I hate poop like that. That's way worse than me!

I absolutely reamed that carb body with carb cleaner and compressed air. New oem mikuni build kit, new fuel filter. I was so confident I loaded it up and drove two hours, dumped it in the water and just took off hoping that I'd got it right. Happy to say that I did!
 
I've experienced the same thing. A crusty old snowmobile carb that is very similar to an sbn. I cleaned it very thoroughly with carb clean and compressed air and even could see light through the progression holes when I shined a flashlight into it but wouldn't run right. Noticed one of the holes was dimmer than the others, more compressed air and carb cleaner wouldn't do it had to give it a poke. Strand of fine copper from an electrical wire wasn't strong enough needed a fine steel wire, that got it, nice bright light through the hole, and then it ran great.
 
If you are doing an new engine or new top-end because the old one failed. #1 is the rebuild the carb. Lucky it didn't cost you a new engine.

I lost my old top end because I lost my cooling line. Got it as a running ski and it didn't give me a single issue all year - I promise you'd have never guessed it looked like that in the carb if you rode it.

Anyway, just one of those things I guess.
 
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