- Location
- Folsom, CA
Ok so in a nutshell my neighbor bought a couple 550's and it has been a nightmare trying to get them to run. I'll focus on just one of them right now since it's the closest one I've got to running. Basically I'll just say what I've done already and hopefully someone knows how to fix this. The ski is an 88 with a 550 piston port motor.
It all started with just rebuilding the carb in an attempt to get it running until I found out the crank seals were bad. Tore apart whole motor, replaced all the crank seals and put fresh gaskets on everything and even replaced the rings. Used Permatex copper gasket sealer on the head gasket, base gasket, and all the exhaust gaskets. All still stock exhaust. Used regular red permatex gasket sealer on all the intake gaskets. Like i said the carb has already been rebuilt as well which is a stock BN44. All the fuel likes have been replaced as well as the pulse line and I even bypassed the petcock selector for reserve or main just in case it's leaking. Checked the check valve and its operating correctly.
Got it all back together and went out to the lake yesterday and no matter what I do with the settings on the jets it will not rev past half throttle and if i try holding it past half throttle it will just bog down and shut off. It will fire up and idle, but acts like its leaning out past half throttle. I've tried setting everything back at factory settings for the carb and no change. I looked around online and some people say timing could do this which I set back to what it was at before I tore the motor apart, or it could be something with the restrictor for the fuel return. It currently has the factory inline restrictor with that little hose that runs to the side of the carb. Can those go bad?
I really hope someone can point me in the right direction cuz at this point I'm about to set the damn thing on fire and watch it sink. I've got a 750, 650, 440, and a 300 and have never had so many issues one after another, but of course it has to go that way when you are trying to help someone else out right? The ironic thing is he bought the 750 I now own with the 2 550's and the 750 fired right up after a carb rebuild and the 2 550's have been a total nightmare to get running lol
It all started with just rebuilding the carb in an attempt to get it running until I found out the crank seals were bad. Tore apart whole motor, replaced all the crank seals and put fresh gaskets on everything and even replaced the rings. Used Permatex copper gasket sealer on the head gasket, base gasket, and all the exhaust gaskets. All still stock exhaust. Used regular red permatex gasket sealer on all the intake gaskets. Like i said the carb has already been rebuilt as well which is a stock BN44. All the fuel likes have been replaced as well as the pulse line and I even bypassed the petcock selector for reserve or main just in case it's leaking. Checked the check valve and its operating correctly.
Got it all back together and went out to the lake yesterday and no matter what I do with the settings on the jets it will not rev past half throttle and if i try holding it past half throttle it will just bog down and shut off. It will fire up and idle, but acts like its leaning out past half throttle. I've tried setting everything back at factory settings for the carb and no change. I looked around online and some people say timing could do this which I set back to what it was at before I tore the motor apart, or it could be something with the restrictor for the fuel return. It currently has the factory inline restrictor with that little hose that runs to the side of the carb. Can those go bad?
I really hope someone can point me in the right direction cuz at this point I'm about to set the damn thing on fire and watch it sink. I've got a 750, 650, 440, and a 300 and have never had so many issues one after another, but of course it has to go that way when you are trying to help someone else out right? The ironic thing is he bought the 750 I now own with the 2 550's and the 750 fired right up after a carb rebuild and the 2 550's have been a total nightmare to get running lol