Races were great. Freestyle sucked again this year.
No pros and 2 amateurs one of which was a 550 lol. Which I think I enjoyed better.
BK you should have competed. If I had my old superjet I would have, I would have at least came in 3rd haha.
It is only a jetworks 861 7 mill stroker that I had blue rebuild this spring. It now runs amaxing after getting the right jetting. Standard compression with 35cc domes.
It just seems that it is too new at the moment. People are trying different configurations to see what works best,new water...
Thats the way it always goes. There is no load on the engine.
Seems to have a lot of scoring on the cylinder walls for new pistons. Whats the compression?
Did you disconnect the overheat sensor from the ebox after the new head?
You can turn the air mixture screws to a 1/8-1/4 turn out and start from there. If it runs better then you know what direction to go on jetting.
You will have steam come out of the bypass or a clean piston if its a head gasket.
This thread is the reason I am scared to swap to a laydown down pipe. I know there is more power to gain but it isn't worth the cost of constantly tuning. It is just too much of an unknown what works for each set up. After watching that recent video of the guy with a 1200 stock electronics and a...
Success!
Turned both screws in to 1/2 turn each to start over.
Damn if the thing ran good. Just need to fine tune a bit and see if I can adjust the throttle cable. Still has the rpms loss to the left and rpm gain to the right.
I will miss having to choke my chicken. Maybe I will get good head...
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